CLC85TA
Forum Member
Anyone use them? know of them? are they a quality gasket?
It seems I just blew apart my 2nd one in my car this summer. I have yet to get under the car, but last night when I got home from taking my old man for a spin, I parked the car in the driveway idling and moved stuff out of the way so I could park the TA. When I got out I noticed a 8" puddle in the driveway, along with a heavy trail of drops leading down to the garage. There were no trails or drops to speak of when I pulled the car out, or coming in or out of the driveway. What gives?
I have put about 25 miles on the engine since I replaced the gasket. Both sides were RTV'd and let set. The first gasket disintegrated when my Holley carb dumped about 2 quarts of gas into the carb and I didn't have time to take care of it. The entire rear hoop over the rear main adapter had disintegrated, most of which ended up in the pickup screen for the oil pump.
The motor originally had a Fel-pro gasket, but it over hung the skirts of the block and seemingly was snagged by the crank at some point.
I'm getting disappointed with this motor, anyone have any suggestions aside from making my k-member a 3 piece unit?
It seems I just blew apart my 2nd one in my car this summer. I have yet to get under the car, but last night when I got home from taking my old man for a spin, I parked the car in the driveway idling and moved stuff out of the way so I could park the TA. When I got out I noticed a 8" puddle in the driveway, along with a heavy trail of drops leading down to the garage. There were no trails or drops to speak of when I pulled the car out, or coming in or out of the driveway. What gives?
I have put about 25 miles on the engine since I replaced the gasket. Both sides were RTV'd and let set. The first gasket disintegrated when my Holley carb dumped about 2 quarts of gas into the carb and I didn't have time to take care of it. The entire rear hoop over the rear main adapter had disintegrated, most of which ended up in the pickup screen for the oil pump.
The motor originally had a Fel-pro gasket, but it over hung the skirts of the block and seemingly was snagged by the crank at some point.
I'm getting disappointed with this motor, anyone have any suggestions aside from making my k-member a 3 piece unit?